I have done what you said on fully functioning board.
And the result is same.
Also I found some new one.
After enabling the device and before configuring it to 1x mode(with debug mode), I spun the motor with my hand right, it spun like crazy.
I guess hall sensor is acting like PWM to 6x mode. : I also tied INCL low here.
Anyways. tieing INCL low is not working for me.. :(
I look forward to hearing from you.
And the result is same.
Also I found some new one.
After enabling the device and before configuring it to 1x mode(with debug mode), I spun the motor with my hand right, it spun like crazy.
I guess hall sensor is acting like PWM to 6x mode. : I also tied INCL low here.
Anyways. tieing INCL low is not working for me.. :(
I look forward to hearing from you.